PJ2T 2006-07 Antenna Rebuild Project

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On June 26, 2006 the boom of the PJ2T 15 meter Europe monobander broke overnight, hanging itself and the reflector at a crazy angle, still somehow attached to the antenna. I (W0CG) managed to lasso it and break it loose from the top of the tower and got the corpse (photo at right) to the ground.

It was quickly apparent that salt-catalyzed dissimilar metal corrosion had eaten through the boom where the overhead boom truss was attached with a U-bolt. Panic ensued as I realized that nearly every one of our yagis was in similar jeopardy because there were other places where steel and aluminum were in contact. The antenna had been in the air for five years. 

It hit us in CCC that almost all of the antennas would have to come down and be significantly rebuilt. In addition, most of the guy wire tails (the bottom 15 feet or so that weren't Phillystran) were corroding badly and needed replacement. Nearly all of the hardware was becoming a mass of rust in spite of our best efforts to coat and otherwise weatherproof all this stuff. 

Thus began a fairly massive 18 month rebuild project, very costly in dollars and in labor time. And we had to do this project concurrent with the non-stop processes of tower painting and inside repairs of equipment and computers. 

 Please have a look at our work plan and photo album. Note the captions at the bottom of each photo. 

Click Here for Work Plan        Click Here for Photo Album


Problems Fixes
Here were the problems:
  • Most antennas had a very small minority of steel parts which we used reluctantly but by necessity in 2001 when they were assembled, and all of these were eating the aluminum they were in contact with.
  • All Hy-Gain boom to mast mount blocks had welded themselves together -- stainless hardware was welded into the aluminum blocks permanently by the salt.
  • All of the ancillary hardware in the air and on the ground to stop torsioning of the booms in wind, including lots of turnbuckles and wire clips, were frozen masses of rust in spite of our best efforts to protect them from the salt.
  • Nearly all guy wire tails, which were 1/4 inch EHS, were rusting badly, along with their deadends, and were approaching failure. (Our guys are mostly Phillystran, but the bottom 15 feet are steel to prevent fire, abrasion, and vandalism damage.)
  • Many of the stainless steel parts were corroding and locking up, including quite a few spring clips. 

 

Here's how we fixed these, in summary.
  • Prepared a detailed 17 page schedule of work and materials needed.
  • Designed and fabricated custom subassemblies for all antenna rebuilds, including new side mount brackets, pictured in grey in the background of this web page. 
  • Made a plea to members for help, finally deciding to do the repairs incrementally as contest teams were available and on site rather than trying to do it all in one massive "fix" trip. 
  • Passed the hat to fund the project. All told we spent about $5000 on parts and materials, most of which funding was donated by NP2L. DX Engineering parts, especially the saddle clamps, saved our lives and made this project possible.
  • Bag-dragged parts to the island in many checked airline bags over several months' time.
  • Obtained six Hy-Gain boom end pieces from N8NR's ice storm destroyed antennas and took them to Curacao in a huge 8 inch PVC tube on the airlines.
  • Took down the Europe 10 (with an electric grinder) in September 2006 using a non-ham friend of W0CG's and his girlfriend to handle ground ropes.
  • Replaced all ground components in the Europe tower boom guys in September 2006. 
  • Began one by one replacement of guys with new deadends and EHS, coating it all in epoxy, tape, and putty. (See photos.) Each one took a day and a half.
  • W0CG rebuilt this antenna in about a week of long days. It was torn down to the smallest pieces, and every bolt and strap was cleaned and replaced where necessary.
  • Parked this antenna at 20 feet so it would not be stolen while CG was gone.
  • Installed all three sets of the new sidemounts on the Europe tower.
  • Installed splints in the legs of the WARC tower at the rotor plate, as the plate U-bolts were eating through the aluminum tower legs.
  • Took down the Europe 15 (grinder) after CQWW SSB with help from N6ZZ (SK) and his friends and W4PA on the tower and put it in a closet, disassembled, for safe storage while off the island.
  • Rebuilt the Europe 15 prior to CQWW CW 2006 with many hours of labor from K8ND, W0CG, W0NB, NP2L and others.
  • Took down the Europe 20 (grinder) with help from W8WTS.
  • Rebuilt the Europe 20, finishing it the day before the contest and put it back up on the new sidemounts.
  • After CQWW put the Europe 15 yagi back up on a new sidemount.
  • Put the Europe 10 back up using a non-ham friend of CG's and his XYL in December 2006.
  • Continued guy tail replacement as time permitted, with help from WB9Z, N8LGP, and whoever happened to be standing around.
  • Lowered the US top 10 and then took down the US/JA 15 in July 2007 with help from DL6LAU and his crew of PJ2HQ Germans.
  • CG totally rebuilt the 15 yagi, requiring four and a half full days of work. Most parts had to be cut off with the grinder.
  • Put the 15 yagi back up on the last day the DLs were available in July.
  • Lowered the 10, took down the US 15, then took down the US 20 in November 2007 after CQWW CW with W8WTS on the tower.
  • CG and K8ND rebuilt the US 20 (two and a half full days).
  • Put the 20 and 15 back up on Wednesday after CQWW CW.
  • Reattached all ground wind guys and lateral guys over the next three days.
  • Except for five more guy tail replacements (none are critical) the project is complete, 18 months and hundreds of parts and subassemblies later.

 

 

Keys to Survivability in Salt Air -- Lessons Learned at PJ2T:

  • There's salt suspended in the invisible wind-driven micro-droplets, so the key is don't let them touch any metal that may be corrosive.
  • On antennas, avoid steel wherever possible and use only top grade stainless and aluminum.
  • Where steel can't be avoided, such as galvanized wire clips or guy wire dead ends, paint it, completely pot the assembly in duct seal putty (Home Depot electrical department), wrap it in Scotch 33, then varnish the tape
  • The photo at the right shows a large 403 porcelain guy wire insulator that transitions from Phillystran to EHS steel, completely potted, taped, and varnished.
  • Paint guy wires with two coats of epoxy, avoid abrasion damage while installing, then paint dead ends after installation with epoxy, pot connections in putty, then tape and varnish the outside. Yes, this means taping the entire exposed length of guy wires!
  • Absolutely avoid steel and aluminum in direct contact anywhere in the tropics. 
  • We use literally hundreds of 1 pound bricks of duct seal and rolls of Scotch 33 tape. 
  • Never ever install anything threaded without first coating the threads with NAPA anti-seize.

 

August 10, 2006: Steve, N8LGP working in his machine shop at home on antenna rebuild kits for PJ2T

We bought lots of components from DX Engineering. The quality is incredible. Here Steve's cutting apart a large DX Engineering flat plate to make some of the boom side mount assemblies.


And yes, it's absolutely worth it. At times during CQWW CW 2007 we were logging 10 QSOs/minute in Multi/2 on 40 and 80. That's funnnn!!